B-17F Crashes and Burns
Four Miles South of Mineral Wells
By Jeff Clark
“Thank you
for your request. Attached is a copy of the accident report covering the loss
of B-17F, s/n 42-5719, at Mineral Wells TX on 11 March 1943…We hope this
information is of value to you.”
I’m staring
at a faded copy of a “War Department – U.S. Army Air Forces Report of Aircraft
Accident.” The men flying that plane are no longer around to interview. This
sheaf of papers will have to tell their story.
First Lieutenant
Jack A. Nilsson; 2nd Lieutenant William F. Pitts of March Field , California ;
2nd Lieutenant Morgan A. Regan; Staff Sergeant James F. Deaver of
Bluff Dale, Texas ;
Sergeant Jamieson P. Ware of Dallas ;
William R. Thaman of Ohio ;
Corporal Olen G. Diggs of Lubbock
and Private Joseph F. Yonack of Dallas
are recorded on the Personnel Listing.
Nilsson was
Pilot Instructor for the training mission, with Pitts and Regan on board as
student pilots. Five enlisted men rounded out their crew. All were stationed at
the Army Air Forces Advanced Flying
School , members of the
955th School Squadron, Hobbs Field ,
New Mexico .
There is an
extensive listing of damage, of what investigators found smoldering on the
ground. By the time you read this, this plane crash’s anniversary will be two
weeks away.
The men’s
B-17F is known as a “flying fortress” four-engine heavy bomber, developed in
the 1930s, a high-flying aircraft able to suffer massive combat damage and still
stay in the air. The B-17 dropped more bombs than any other aircraft type
during WWII.
This fated
plane took off from Hobbs Army Air base on a navigational training flight March 11, 19 43 at about 1500 hours.
The crew received clearance to fly at 8,500 feet to Amarillo, then Tulsa, Shreveport,
turning east to Dallas and then on to Fort Worth, where they were to RON
(remain over night), returning to Hobbs the following day.
Nilsson
writes, “I knew the weather was bad at Fort Worth…We had approximately 2,500
gallons of gasoline aboard and only a 6 ½ hour flight to make.” They pushed
along at 180 mph for the first two hours, hoping to beat worsening weather developing
around Cowtown.
Nilsson
recalculated fuel consumption. “I discovered we were consuming it at an extravagant
rate”. They throttled back to 1,850 RPMs. Speed dropped to 160 mph.
As they
approached Amarillo
around 1615 hours, transmitter trouble prevented them from making radio contact
until they were 40 miles east. They were told to proceed to Tulsa . About 60 miles southeast of Tulsa , electrical storms
prevented them from keeping radio contact with Shreveport . Nilsson relates “the static was
so severe that we couldn’t hear the S.
P. Range .
We climbed to 14,000 feet in order to get on top of the overcast.” They finally
reestablished radio contact.
The report states that except for
“excessive fuel consumption and increasingly bad weather,” the flight was
normal until the plane left Shreveport .
It began to pick up ice. The pitot tube froze (used to measure air speed), but pilot
heat was turned on and the instrument came back online. The pilot lifted the
plane to escape icing and to maintain radio contact. Student Pilot Pitts said,
“My radio would go out when I got into the clouds. We got over Shreveport so we could follow the beam and
this side of Shreveport
we ran into an electrical storm…When I got into the overcast, the radio
wouldn’t work at all.” Rounding Shreveport ,
the plane turned east toward Dallas .
Cruising at
14,000 feet on the way to Dallas ,
they ran into large build ups of clouds and again started to pick up ice. They
had to climb to 18,000 feet to get above the icing and retain radio contact.
As they
approached Dallas ,
they dropped down into the overcast at 14,000 feet. They maintained radio
contact this time. When they were over Dallas Radio Station at 2030 CWT , the ceiling in Fort Worth was reported at 800 feet.
Pilot Pitts
remembered, “As we came into Fort Worth and went on out the north leg for
procedure let down, the ceiling dropped to 300 feet and in a very little while
it was down to 100 feet and he told us to go to Abilene. As I was going around
to make a 180 degree turn to come back onto the beam, my No. 1 engine went out….we
were at 3,000 feet then.” The three-bladed prop fell silent.
Nilsson reached down between his
student pilot and copilot and pushed the feathering button to reduce drag. The
oil pressure slowly dropped to 30 lbs. They were advised there was an airliner
coming in underneath them somewhere.
The crippled plane managed to climb
to 8,000 feet on their three remaining engines. They only had 600 gallons
remaining, enough for two more hours of flight. Nilsson transferred the gas
from their silent No. 1 engine to the remaining three engines. He believed he
could make it all the way back to Hobbs
if he had to.
“The co-pilot and I trimmed ship as
fast as possible, with full right rudder,” Pitts said. “Both of us were
standing on the rudder. At the same time we were trying to maintain altitude.”
The weather outside continued to
worsen.
About that time the No. 2 engine
went out. It would not feather. Pitts called for full power on the remaining
two engines. He called out that he needed help controlling the aircraft.
Co-pilot Lt. Regan “gave all the help he could to the pilot by helping him hold
full right rudder and setting the trim tabs in an effort to keep the airplane
flying straight and level.” It made two complete turns to the left.
The left side of the plane was
silent.
The right side rumbled and screamed
aloud under full power.
Pitts wrote, “I was watching the
flying instruments at the time but I knew No. 2 was out when I felt the plane
lurch.” The left wing lowered. They were fighting to keep their aircraft level.
Pitts lets
us look over his shoulder. “We asked (Fort Worth) for emergency landing fields
and they wanted to know where we were. We couldn’t give our exact location
because we were going around in circles with little fuel left and a 100 foot
ceiling all around.”
They only had
500 gallons of fuel left.
Nilsson
attempted to contact Abilene
by radio, but couldn’t. Regan tells us, “We continued to try to get the Abilene beam. Lt. Nilsson
had tried several times to set the radio but we could only get “jumble”. We
reported this fact to the Fort Worth
radio and asked for instructions but didn’t get any.”
The men
were alone.
The pilot
and copilot were unable to control the plane. They were going down. Air speed
fell to 115 mph. They couldn’t keep a compass heading. Nilsson estimated they
were 50 miles from Fort Worth
with a ceiling no more than 600 – 800 feet.
“I decided
to abandon the airplane,” Nilsson said. He told the engineer to get the crew
into their parachutes and to stand by for his command to jump.
“I pulled
the emergency release and opened the bomb bay doors and dropped the bomb bay
tanks.” The plane had fallen to 6,000 feet.
“Jump!”
Nilsson
signaled Lt. Regan to “tell pilot Lt. Pitts to cut the switch and then jump
through the bomb bay. Lt. Pitts forgot to cut the switch before jumping.”
Nilsson was the last to leave the doomed aircraft.
He floated
down, finally getting below the overcast. He could see the lights of Mineral
Wells off to the north. He hit the ground hard, spraining his ankle and left
foot. “I hobbled to a highway and a car stopped who had already picked up Lt.
Pitts. By this time the Fire Department and the Highway Patrol had arrived. I
gave them the names of the crew so they could be found and picked up. The
airplane crashed three or four hundred yards from where I landed.”
Four miles south of Mineral Wells their
downed B-17F warbird lay aflame in a scrub oak pasture. The Engineering Section
at Patterson Field , Ohio later examined the power plants and
diagnosed the cause of the crash as “dust”.
I’m still reading the report, my
fingers gripping the 68-year-old report a little too hard. “First Lt. Jack A.
Nilsson is to be highly commended for the coolness displayed in this emergency,
and for evacuating his crew in sufficient time to prevent loss of life.”
Regan later
tells that this plane had made a previous trip to Santa Ana where their No 4 engine went out.
They were able to feather it and land at Williams Field. I was thankful this
crew survived their trial in the skies above Mineral Wells.
Researching
this story I began to find that mechanical failures and a “just make it work” mindset
was SOP back then. We were at war. Get in the air. Get in the fight.
2nd Lt.
Pitts later became Lt. General William F. Pitts. He retired in 1975 with a staggering
list of accomplishments including Commander of the Fifteenth Air Force,
Strategic Air Command headquartered at March Air Force Base, CA. Their mixed
force of recon aircraft and bombers, along with missiles, conducted operations across
the Western U.S. and Alaska .
General Pitts was born at March
Field, now March Air Force Base, CA in 1919. He was chief of the Senate Liaison
Office for Secretary of Air Force. He commanded the 327th Air
Division in Taiwan ,
was chief of the Air Force Section of the Military Advisory Group to the
Republic of China, was Commander of Third Air Force, U.S. Air Forces in Europe , stationed in England . He led the Sixth Allied
Tactical Air Force Commander in Turkey .
General Pitts received many decorations and awards.
Back in the final months of WWII,
Pitts went to Tinian
Island in the Marianas with his squadron where he flew 25 missions
against Japan
as lead crew commander in B-29s. Pitts’ training commander from that Mineral
Wells crash landing Capt. Jack A. Nilsson also flew B-29 missions from the Marianas . Surely the two men saw each other there.
Nilsson’s
crew number 41 plane that night was tagged T46. Its roster included, Capt. Jack
A. Nilsson, Pilot 1st Lt. Adolph C Zastara, Navigator 1st
Lt. Eric Schlecht, Bombardier Capt. Loyd R Turk, Flight Engineer 2nd
Lt. Daniel J Murphy, Radio Operator S/Sgt Eugene P Florio, CFC Gunner T/Sgt Faud
J. Smith, Left Gunner T/Sgt. Robert Starevich, Right Gunner Sgt. Joe McQuade, Radar Operator S/Sgt. Norbert H Springman, and Tail Gunner
S/Sgt. John C. DeVaney.
“All
aircraft bombed the primary target visually with good results.”
Nilsson’s plane came under heavy
fire, crashing during their bombing run against the City of Toukyou on May
24, 19 45 , one kilometer off the east coast district of Oomori,
Tokyo Haneda. Nilsson was thought to be the pilot at the time. His plane was
one of 17 B-29s lost that day on Mission
181. His body was never recovered.
One man who
walked out of that 1943 Mineral Wells pasture went on to lead thousands in the
defense of this nation for over four decades, all over the world. Another gave
his life over the skies of Tokyo
6,410 miles west of Palo
Pinto County .
Heroes walked among us.
Special thanks to O. B. “Butter” Bridier, to the Department of the Air
Force, Air Force Historical Research Agency, Maxwell Air Force Base, Alabama,
to Richard “Doc” Warner, Civ, USAF 7th Bomb Wing Curator/Historian
(Dyess AFB), Rae Wooten, Michael Manelis, and to
Paul G. Ross, whose father James S. Ross was shot down the same night as Capt.
Nilsson.
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